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Please take the time to describe the issue in detail, so that other contributors can pick it up and implement or declare it done/obsolete in case it was fixed out of band.
Current behaviour/situation
Because the rotor is press-fit onto the stepper motor shaft, differences in 3D printing settings and material can result in some parts not fitting correctly, which results in loose, wobbly rotor.
Expected state/behaviour
Tweak for optimal material and print settings and provide these in the documentation for repeatable results.
Rotor model should be updated if needed.
How do you know it is wrong
Anecdotal observation during integration.
Starting points
Print and test rotor fit on a stepper motor
Don't forget (can delete these when done)
Put the issue in a milestone
Assign it to one of the projects
Add appropriate labels
Mention dependent/blocked issues if any
The text was updated successfully, but these errors were encountered:
Please take the time to describe the issue in detail, so that other contributors can pick it up and implement or declare it done/obsolete in case it was fixed out of band.
Current behaviour/situation
Expected state/behaviour
How do you know it is wrong
Anecdotal observation during integration.
Starting points
Don't forget (can delete these when done)
The text was updated successfully, but these errors were encountered: